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A Study on the Design Improvement to prevent the stoppage phenomenon of Launch Support Device for Self-Propelled Artillery

자주포용 발사지지대의 멈춤현상 방지를 위한 설계개선 연구

  • Kim, Sung Hoon (Land Systems Center, Defence Agency for Technology and Quality) ;
  • Park, Young Min (Land Systems Center, Defence Agency for Technology and Quality) ;
  • Noh, Sang Wan (Land Systems Center, Defence Agency for Technology and Quality) ;
  • Park, Dae Hoon (System Engineering Team, Hanwha Defense)
  • 김성훈 (국방기술품질원 기동화력센터) ;
  • 박영민 (국방기술품질원 기동화력센터) ;
  • 노상완 (국방기술품질원 기동화력센터) ;
  • 박대훈 (한화디펜스 체계기술팀)
  • Received : 2020.01.22
  • Accepted : 2020.05.08
  • Published : 2020.05.31

Abstract

This paper reports a design improvement study to solve the stoppage phenomenon caused by the launch-support device applied to K105A1. The K105A1 is a weapon system equipped with an old 105 mm towed howitzer in a wheeled vehicle, which provides superior maneuverability compared to track equipment. The launch support device serves to withstand fire impact and load. In this way, this device is fixed firmly to the ground in preparation for the shooting mission and is responsible for the critical performance, such as fixing the position of the vehicle. On the other hand, during the field test, a temporary stoppage of the launch support occurred, which caused a problem of not being fixed to the ground. To solve this problem, the cause of failure was analyzed by a replay test and parts inspection. In addition, the operating concept, method, and design were analyzed to derive the cause and solve the problem by changing the parts design. Finally, the performance and firing missions were performed normally by applying the changed design to K105A1. The performance stability and reliability of the launch support device were confirmed, which are expected to be of great assistance in the development of military equipment in the future.

본 논문은 K105A1자주포에 적용중인 발사지지대 장치에서 발생한 하강운용간 멈춤현상을 해소하기 위한 설계 개선에 관한 연구이다. K105A1자주포는 기존의 105mm 견인곡사포를 차량에 탑재하여 기존의 궤도장비보다 신속한 기동성을 확보한 무기체계로써 사격충격력 및 부하를 지지하기 위해 발사지지대가 적용되어 있다. 이러한 발사지지대는 사격 전 지면에 단단히 고정되고 사격제원 유지, 차체 자세제어 등 사격임무 수행에 중추적인 역할을 하여 성능발휘에 대한 높은 신뢰성이 요구된다. 그러나, 야전운용시험 간 발사지지대를 설치하는 중 간헐적인 멈춤현상이 발생하여 지면에 고정되지 못하는 문제가 발생하였다. 이러한 문제를 해소하기 위하여 야전에서의 재연시험 및 부품단위 분해검사를 통해 고장원인을 분석 및 검토하였다. 더불어 발사지지대의 운용개념, 작동 메커니즘 및 구성품 단위의 설계분석을 통해 근본적인 원인을 도출하고 이를 해소하고자 관련된 부품의 설계를 변경하여 발사지지대의 멈춤현상을 해소하였다. 마지막으로 설계변경사항의 효과성을 확인하고자 완성체계 상태에 적용하여 발사지지대 성능 및 사격임무 수행이 정상적으로 이루어짐을 확인 및 입증하였다. 이에 따라, 본 연구에서는 K105A1자주포 발사지지대의 성능에 대한 안정성 및 신뢰성을 확보하였으며, 본 연구가 향후 군용장비 및 유사품목 개발시 많은 도움이 될 것으로 기대된다.

Keywords

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